Thanks Peter from Australia for sharing with his mTech 3i on his Cougar Mill/Drill
He is using scale travel "220mm, 370mm and 420mm)
Below is the complete write-up by Peter:
INSTALLATION OF THE TECH-3i DRO ON MY COUGAR MILL/DRILL
This Chinese machine is is built to the   popular ZX7550C pattern. It was built in around 2003. 
I obtained it several years ago, from a   manufacturer in Sydney who never used it, before winding up the business.  
My   first task was to bring the machine into the workshop from it's storage in the   garage.
The X-axis position provided good machined   surfaces and access. 
The placement of the scale and it's cover   restricts Y-axis travel by about 60mm, 
so that a new stop was later fitted. All   that was required to get final alignment was a shim behind the reader.   
The Y-axis field left something to be   desired. (See below.)    
Firstly, the surfaces are painted with thick,   uneven enamel. 
Secondly, the area is barely wide enough to   accommodate the scale, so the cover cannot be used. 
For the scale I scraped all the paint off   the surface, and mounted the scale as low as possible to 
give me a narrow lip above for some   protection to be devised in the future.    
After some shims to correct alignment the the   scale sits very nicely.
The reader was mounted using some of the   machined aluminium plates provided in the excellent kit from TheDroStore.com. 
To the right of the scale you may be able   to see a tapped hole on the mill. I decided to use a piece of aluminium   channel  as a shield.   
I am machining part of one side out of the   channel to accommodate the scale body 
and   will attach the remaining complete channel side, using the tapped hole   indicated. 
A similar hole will be drilled to the left   of the scale after preliminary fitting. 
Throughout the install, there were   lubrication ports to be preserved. 
I was surprised this did not cause any   problems.  
Also   I managed to dodge the slide locks on opposite faces of the   machine.
Fitting the Z-axis presented the paint   problem once again. This time, however, I used a slightly different approach.   
By scraping the paint carefully, I managed   to obtain a usable surface, and with the help of suitable shims,   
the test indicator (seen above) proved that   scale alignment was satisfactory. 
Once again the aluminium mounting hardware   provided proved excellent to carry the Z-axis reader. 
A piece of angle, trimmed down, a bit more   paint scraping and a shim mounted on the knee and the job is nearing   completion.
Covers were fitted to the X and Z-axis   scales, with a small plate glued to the top of the Z-axis cover to help   
protect it from falling coolant and swarf.   (See below.)
Installing the readout went smoothly.  Suitable positions were available and a   transformer in the pedestal 
provides 240v to power the display. The   last photo shows the display in use and on the table the 
shield for the Y-axis scale partly   machined. 
This is my very first milling operation. So   far so good. No broken cutters, etc.
Considering that I have never attempted   anything like this exercise before I am very pleased with the result.   
I must say the kit provided, Scott's   manuals and his other help have been confidence building and a big part   
of completing the task at hand. As many   others have commented, there was a surplus of  materials and a choice of  install methods.
Many thanks,
Peter Browne
Australia











